11063112100 Kenmore Dryer - Instructions
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Dyer drum doesnt turn
It was really quite esy remove the screws from the back and pop the top off . then remove 2 top inside screws from the front , lift the front off the sides , support the drum and lift out , you will then see the idler wheels, replace them with the new ones ,replce the tensioner , wrap the belt around the drum, need help putting the drum back in the case, have someone hold the drum in place while you lay on the ground and put the belt around the motor pulley and the tensioner on the bottom.you then put the front panel back into place and secure with the 2 inside screws, then put the rest back together in reverse oder. ... hope this helps someone
Parts Used:
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Shawn from Akron, OH
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Difficulty Level:Really Easy
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Total Repair Time:15 - 30 mins
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Tools:Nutdriver, Pliers, Screw drivers
27 of 29 people
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had to replace the motor
Follow the advice given in the partsselect website. However, while removing the blower, my hand slipped into the housing and cut my thumb. Connected the wires to the junction box on the motor but didn't realize that the contacts would hit the drum when reinstalled. The original junction box was at a 90 degree rotation relative to the new box. When trying to test the breaker tripped. Using the multitester I found out that I burned out the thermal fuse, and froze the door switch. I replace both those parts and started the dryer and could hear a grinding sound. Inspection revealed that the housing of the motor was rubbing against the drum. Removing the drum yet again, I rotated the housing and replaced the drum. The dryer was finally working well.
Parts Used:
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charles from parker, CO
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Difficulty Level:A Bit Difficult
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Total Repair Time:More than 2 hours
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Tools:Nutdriver, Screw drivers
31 of 43 people
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Drier would not heat
Wife said the drier was not heating. I looked on the internet and found Parts Select. Followed the instructions to test the heating element, thermal cut-offs, and thermostat. This is really easy, you just touch the terminals with the voltage meter to see which ones are not transmitting current (with the drier unplugged). One of the thermal cut-offs was not transmitting current so I ordered the part Sunday night and had it by Wednesday morning and put it on it about five minutes. Steps:
1. Unplug drier
2. Unscrew back of drier
3. Unplug wires from terminals of the parts shown in Parts Select instructions (one at a time)
4. Get a basic voltage meter (I bought a cheap one at the big box store)
5. Test terminals (touch the red terminal on the voltage meter to one side, black to the other)
6. If the needle moves to the other side, the part is OK, if not order the part and replace.
1. Unplug drier
2. Unscrew back of drier
3. Unplug wires from terminals of the parts shown in Parts Select instructions (one at a time)
4. Get a basic voltage meter (I bought a cheap one at the big box store)
5. Test terminals (touch the red terminal on the voltage meter to one side, black to the other)
6. If the needle moves to the other side, the part is OK, if not order the part and replace.
Parts Used:
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Jason from Birmingham, AL
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Difficulty Level:Really Easy
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Total Repair Time:30 - 60 mins
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Tools:Pliers, Screw drivers
26 of 29 people
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Drayer Was Making Squeaking Sound
Took off the top and front panel. Found that the belt tensioner was worn out. Decided to pull drum out,and replace the belt and drum rollers also. Put it back together, and it works fine.
Parts Used:
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Charles from Gray, TN
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Difficulty Level:Easy
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Total Repair Time:1- 2 hours
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Tools:Nutdriver, Pliers, Screw drivers
26 of 30 people
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Dryer would not heat up; blow only air
I replaced the thermal cut off kit, and the dryer now had heat. Three days later, no heat; the thermal fuse also did not have continuity. Read on-line that overheating was the most likely cause. So, I checked the exhaust duct for blockage, but it was clear. Then, I removed the exhaust canister at the back of dryer; the entire bottom was filled with lint the size of a softball. The lint was heating up, and when it got too hot, it blew the thermal cut off. Cleaned out the lint, replaced the thermal cut off, and now it's fine. Moral of the story: Remove the lint canister and clean it.
Parts Used:
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William from Sacramento, CA
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Difficulty Level:A Bit Difficult
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Total Repair Time:1- 2 hours
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Tools:Nutdriver
26 of 30 people
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Dryer would not tumble.
I wasn't sure if the problem was the belt (probable) or the idler pulley assembly (less likely) but the total for both parts was about $26 plus shipping. So why not replace both to be sure?
As it turns out, my original idler pulley assembly does not turn. Rather, it has a concave semi-circular piece that is fixed in place. The belt ran in a groove in that piece.
The replacement part has a nylon wheel that turns. As a result of replacing the idler pulley assembly (which I don't think was necessary to fix my tumbling problem) the dryer runs much quieter. (We used to get a fair amount of squeaking when the belt rubbed).
As for the actual repair (I would rate myself as above average on tackling household repairs), it was about the simplest repair I've ever done. I followed the video provided on this site (excellent video) and it took less than 20 minutes -- cleaning up all of the lint/odds and ends under the washer and dryer took longer than the actual repair.
My only issue (minor) was disconnecting the electric harness. It did not slide as easily as in the video. I had to coax mine a bit with a small screwdriver (make sure your dryer is unplugged!!). I suspect it was simply a function of the harness never being unplugged -- the dryer is 9 years old.
I also felt great because I'm sure I saved a $125 service call (for only $26 in parts and 20 minutes of my life).
Good luck!
As it turns out, my original idler pulley assembly does not turn. Rather, it has a concave semi-circular piece that is fixed in place. The belt ran in a groove in that piece.
The replacement part has a nylon wheel that turns. As a result of replacing the idler pulley assembly (which I don't think was necessary to fix my tumbling problem) the dryer runs much quieter. (We used to get a fair amount of squeaking when the belt rubbed).
As for the actual repair (I would rate myself as above average on tackling household repairs), it was about the simplest repair I've ever done. I followed the video provided on this site (excellent video) and it took less than 20 minutes -- cleaning up all of the lint/odds and ends under the washer and dryer took longer than the actual repair.
My only issue (minor) was disconnecting the electric harness. It did not slide as easily as in the video. I had to coax mine a bit with a small screwdriver (make sure your dryer is unplugged!!). I suspect it was simply a function of the harness never being unplugged -- the dryer is 9 years old.
I also felt great because I'm sure I saved a $125 service call (for only $26 in parts and 20 minutes of my life).
Good luck!
Parts Used:
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John from Minneapolis, MN
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Difficulty Level:Really Easy
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Total Repair Time:15 - 30 mins
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Tools:Nutdriver, Screw drivers
24 of 25 people
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The lint filter was seriously damaged
After the new filter arrived, I took the old filter out, put the newe one in. No tools, no difficulty at all. Actually, the really difficult part of this entire episode was finding the model number on the dryer. It was on the underside of the door.
Parts Used:
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Katharine from Palm Springs, CA
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
26 of 31 people
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Dryer would quit before the end of the cycle
My wife reported that the dryer was not working. I checked it and it seemed to work fine. This went on for about a month or two. Every time I checked it, it started just fine.
Well, she threatened to go buy a new dryer, I took her more seriously. I thought perhaps a thermal protection was the cause. But when I dug into it, I learned that when those trip out, they are permanent (have to be replaced).
I finally noticed loud humming sound the motor made at start-up, when it failed to start turning on one occasion and eventually tripped out the motors thermal protection.
I ordered the new drive motor form PartSelect.com.
Replacing the motor was fairly easy if you like to take stuff apart. One thing that I had not anticipated was that the two foam gaskets on the exhaust duct were dry rotted. I went to my local part supplier to get them. They did not have them in stock. :( While I was there, I asked how much the motor was, they wanted $50 more than PartSelect.com :D
I put it back together without the new gaskets, and it runs like new. I ordered the gaskets from PartSelect and will add them when they arrive.
My wife is happy again, she can bust out the laundry in one day; it had been taking here all weekend.
I learned to take her at her word.
Well, she threatened to go buy a new dryer, I took her more seriously. I thought perhaps a thermal protection was the cause. But when I dug into it, I learned that when those trip out, they are permanent (have to be replaced).
I finally noticed loud humming sound the motor made at start-up, when it failed to start turning on one occasion and eventually tripped out the motors thermal protection.
I ordered the new drive motor form PartSelect.com.
Replacing the motor was fairly easy if you like to take stuff apart. One thing that I had not anticipated was that the two foam gaskets on the exhaust duct were dry rotted. I went to my local part supplier to get them. They did not have them in stock. :( While I was there, I asked how much the motor was, they wanted $50 more than PartSelect.com :D
I put it back together without the new gaskets, and it runs like new. I ordered the gaskets from PartSelect and will add them when they arrive.
My wife is happy again, she can bust out the laundry in one day; it had been taking here all weekend.
I learned to take her at her word.
Parts Used:
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Ernest from Beaumont, TX
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Difficulty Level:Easy
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Total Repair Time:1- 2 hours
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Tools:Nutdriver, Pliers, Screw drivers, Wrench (Adjustable)
24 of 28 people
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Scratches in Surface
This product comes in a bottle with a brush like Liquid Paper. It goes on incredibly easy. A second coat might be needed. I wanted to prevent rust from setting in so I covered the scratches and dings. The paint is a little brighter since my washer is 10 years old but it still looks great.
Parts Used:
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Michelle from Richardson, TX
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
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The dryer belt broke. During the effort to replace the belt it was noted that the lint trap housing seals were in need of replacement.
With the dryer taken apart to replace the broken belt it was obvious that the lint seals had not been working properly due to the excessive amount of lint covering all of the inside surfaces of the dryer. The belt idler pully had also moved from its normal mounting position and was laying at the bottom of the dryer. Because the lint had covered the bottom before the belt broke it was obvious to determine where the idler pully attached to the bottom.
Before cleaning I marked the exact location where the idler pully mounted to the bottom of the dryer.
While waiting for the replacement parts to be delivered a vacuum cleaner was used to remove lint from the inside surfaces of the dryer as well as the old fragments of the lint trap housing seals were removed and surfaces where the new seals would attach were cleaned.
Assembling the dryer with the new belt was a challenge due to the lack of support for the drum while getting the new belt in place, lined up properly, threaded through the idler pully and attached to the motor drive shaft. This is how I installed the new belt:
I used a piece of wood wider than the sides of the dryer, drilled holes that allowed for a piece of cloths line rope to be looped through and used to support the door opening end of the drum.
The drum was set on the seal and rollers at the back of the dryer.
The temporary wood /rope hanger was placed at the front end of the dryer resting on the sides with the top of the dryer raised.
The rope was adjusted until the drum rested on the back rollers and the rope like it would be positioned normally.
The new belt was then gently installed under the temporary support rope and around the drum.
The new belt had many kinks from shipping and was difficult to align with the location on the drum where it needs to ride so small strips of tape were temporarily used to hold the new belt in position until it could be fed through the idler pully and on to the drive shaft.
Several small pieces of a cardboard box were used to shim under the idler pully to hold it in its proper location as well as to make the belt attachment to the drive shaft easier.
With the belt attached, the temporary cardboard shims were removed from under the idler pully.
The front of the dryer was attached .
The temporary board and rope hanger was removed.
The tape that had been placed over the new belt to hold it in proper alignment was removed as the drum was rotated slowly by hand to ensure that all tape was removed prior to closing the top of the dryer.
The seals as well as the remainder of the dryer assembly was completed without any problems.
The dryer ran well for its initial trial spin and has dried several loads of laundry since.
Great parts and support Thankyou
Before cleaning I marked the exact location where the idler pully mounted to the bottom of the dryer.
While waiting for the replacement parts to be delivered a vacuum cleaner was used to remove lint from the inside surfaces of the dryer as well as the old fragments of the lint trap housing seals were removed and surfaces where the new seals would attach were cleaned.
Assembling the dryer with the new belt was a challenge due to the lack of support for the drum while getting the new belt in place, lined up properly, threaded through the idler pully and attached to the motor drive shaft. This is how I installed the new belt:
I used a piece of wood wider than the sides of the dryer, drilled holes that allowed for a piece of cloths line rope to be looped through and used to support the door opening end of the drum.
The drum was set on the seal and rollers at the back of the dryer.
The temporary wood /rope hanger was placed at the front end of the dryer resting on the sides with the top of the dryer raised.
The rope was adjusted until the drum rested on the back rollers and the rope like it would be positioned normally.
The new belt was then gently installed under the temporary support rope and around the drum.
The new belt had many kinks from shipping and was difficult to align with the location on the drum where it needs to ride so small strips of tape were temporarily used to hold the new belt in position until it could be fed through the idler pully and on to the drive shaft.
Several small pieces of a cardboard box were used to shim under the idler pully to hold it in its proper location as well as to make the belt attachment to the drive shaft easier.
With the belt attached, the temporary cardboard shims were removed from under the idler pully.
The front of the dryer was attached .
The temporary board and rope hanger was removed.
The tape that had been placed over the new belt to hold it in proper alignment was removed as the drum was rotated slowly by hand to ensure that all tape was removed prior to closing the top of the dryer.
The seals as well as the remainder of the dryer assembly was completed without any problems.
The dryer ran well for its initial trial spin and has dried several loads of laundry since.
Great parts and support Thankyou
Parts Used:
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Benjamin from WELLS, ME
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Difficulty Level:A Bit Difficult
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Total Repair Time:30 - 60 mins
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Tools:Nutdriver
23 of 26 people
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Belt broke, dryer stopped.
Replaced the belt and the wheels supplied with the kit. I also cleaned the inside of the unit. It looks and works like new.
Parts Used:
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Richard from Groveland, MA
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Difficulty Level:Easy
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Total Repair Time:Less than 15 mins
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Tools:Nutdriver, Screw drivers
24 of 30 people
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Push start and the motor would hum.
**** Remove power cord from the wall****
As said earlier, you will need to lift the top. Drop the two screws holding the lint shoot and pop the top by sliding a screw driver into the corner on the front. Lif tthe top and rest against the wall behid the unit. remove the two (4 total) screws at the top and bottom of the front door assembly.
Place sometin under the front portion of the drum. At this point you'll see the need to clean everything! :) Slide the belt off and around the drum, (take note of the routing it takes.) Remove the drum by gently pulling it towards you. Set it aside. Clean more. :) (It is nice to have a vacuum handy.) At this point you really need to get to the rear of the system. So I tipped the top back down, and spun it around. Removed the rear panel and cleaned some more. (15 years of a lot of lint in there!) Then you'll need to remove the rear cover on the left side, covering the blower impeller. Get read for a whole lot of debris. Vacuum again. So now you have the motor exposed in the front and rear. You need to remove the impeller by turning that clockwise to loosen it. The trick is holding the shaft in place from the front at the same time. I used an old rag and wedged it into the impeller edges and worked it around until it jamed up. Once the rag was wedged pretty good, I went back to the front spun the shaft. Then you can remove the impeller by hand. Vacuum more. You may get by without having to remove the lint shoot completely, but I did just to clean it up more. I did have to remove two screws in the upper corner near the top of the lint shoot. (Basically the hold the back in place.) I took a few notes at this point about the wiring harness. Used a heavier screw driver (standard), You can push down on the clips that hold the old motor in place. Then work it out the front. Clean more. The new motor is not an exact replacement slightly differnt but the instructions with it were ok. Follow them for the correct wiring. You will need to remove one wire and cut and recrimp a spade lug or two. I used ty-wraps to secure the lines back in place. Look closely at the diagrams and make sure you set the motor down in the same direction the instructions say, if you twist it slightly it will sorta lock in place where it needs to be. Re-install the hold down clips to the front and rear of the motor. Clean up your impeller, and reinstall it too. Then basically reassemble the dryer...tracing your steps backwards. This isn't really difficult, it just takes time and as you can see, you will/should clean as you go !
As said earlier, you will need to lift the top. Drop the two screws holding the lint shoot and pop the top by sliding a screw driver into the corner on the front. Lif tthe top and rest against the wall behid the unit. remove the two (4 total) screws at the top and bottom of the front door assembly.
Place sometin under the front portion of the drum. At this point you'll see the need to clean everything! :) Slide the belt off and around the drum, (take note of the routing it takes.) Remove the drum by gently pulling it towards you. Set it aside. Clean more. :) (It is nice to have a vacuum handy.) At this point you really need to get to the rear of the system. So I tipped the top back down, and spun it around. Removed the rear panel and cleaned some more. (15 years of a lot of lint in there!) Then you'll need to remove the rear cover on the left side, covering the blower impeller. Get read for a whole lot of debris. Vacuum again. So now you have the motor exposed in the front and rear. You need to remove the impeller by turning that clockwise to loosen it. The trick is holding the shaft in place from the front at the same time. I used an old rag and wedged it into the impeller edges and worked it around until it jamed up. Once the rag was wedged pretty good, I went back to the front spun the shaft. Then you can remove the impeller by hand. Vacuum more. You may get by without having to remove the lint shoot completely, but I did just to clean it up more. I did have to remove two screws in the upper corner near the top of the lint shoot. (Basically the hold the back in place.) I took a few notes at this point about the wiring harness. Used a heavier screw driver (standard), You can push down on the clips that hold the old motor in place. Then work it out the front. Clean more. The new motor is not an exact replacement slightly differnt but the instructions with it were ok. Follow them for the correct wiring. You will need to remove one wire and cut and recrimp a spade lug or two. I used ty-wraps to secure the lines back in place. Look closely at the diagrams and make sure you set the motor down in the same direction the instructions say, if you twist it slightly it will sorta lock in place where it needs to be. Re-install the hold down clips to the front and rear of the motor. Clean up your impeller, and reinstall it too. Then basically reassemble the dryer...tracing your steps backwards. This isn't really difficult, it just takes time and as you can see, you will/should clean as you go !
Parts Used:
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Doug from Manitowoc, WI
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Difficulty Level:Easy
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Total Repair Time:1- 2 hours
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Tools:Nutdriver, Screw drivers, Socket set, Wrench (Adjustable)
22 of 26 people
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No heat
Everything seems to work on the electric/gas dryer, but would not generate any heat. Did some research and ordered the thermal fuse & thermostat based on that. Replacement was simple and went well, however it did not fix the issue. Should have checked the continuity first as I found the "replaced parts" to be good. Have checked all other possible symptoms except the heating element, which requires addition labor. Overall, partselect portion was as advertised. All parts arrived quickly and were priced fair.
Parts Used:
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Jaime from Chantilly, VA
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Difficulty Level:Really Easy
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Total Repair Time:15 - 30 mins
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Tools:Nutdriver
27 of 42 people
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The dryer was making a squeaking sound when running
Installation went very well. Raised the top of the dryer, removed the front of the dryer, remove the drum, at this point the dryer‘s wide open removed the police and the tensioner also remove your tire rings replace everything back in order as how are you get apart. Repair took about an hour and 15 minutes
Parts Used:
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David from PATASKALA, OH
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Difficulty Level:Easy
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Total Repair Time:1- 2 hours
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Tools:Nutdriver, Pliers, Screw drivers
21 of 24 people
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Drum would turn but not heat.
After tearing the back off by removing the numerous 1/4 inch hex screws, and locating the schematic in the compartment behind the dryer controls, I took a multimeter on the resistance setting and tested all the components I deduced were part of the heating circuit until i found the upper limit temp fuse of was open (i.e infinite , OL, how ever your meter will display this). I ordered the kit from here and upon installation found I had a different type of Thermistat assembly then the kit came with, however, the kit did anticipate this might happen and had "some" instruction on modifying the wire harness to accommodate the part. Essentially if you have this older style you will need to do some basic wire stripping and crimping to make it all work. While I am an electrical technician on aircraft, anyone should be able to follow the how-to video on this page(which deals exactly with what I had) and with the proper tools install this part.
I also cleaned out and inspected the rest of the dryer since I had it all open, including looking for burning on the heating element and inspection of the rest of the wiring harness. Finally removed the lint chute by removing the two screws located under the lint basket door, and the nuts holding it to the dryer frame and did a work over on it, finding a lot of compacted lint and debris inside. A can of compressed air helped a lot for this.
I also cleaned out and inspected the rest of the dryer since I had it all open, including looking for burning on the heating element and inspection of the rest of the wiring harness. Finally removed the lint chute by removing the two screws located under the lint basket door, and the nuts holding it to the dryer frame and did a work over on it, finding a lot of compacted lint and debris inside. A can of compressed air helped a lot for this.
Parts Used:
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james from corpus christi, TX
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Difficulty Level:A Bit Difficult
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Total Repair Time:15 - 30 mins
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Tools:Pliers, Screw drivers, Socket set
20 of 22 people
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