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7MWGD1602AW0 Whirlpool Dryer - Instructions

All Instructions for the 7MWGD1602AW0
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Drayer Was Making Squeaking Sound
Took off the top and front panel. Found that the belt tensioner was worn out. Decided to pull drum out,and replace the belt and drum rollers also. Put it back together, and it works fine.
Parts Used:
Dryer Maintenance Kit
  • Charles from Gray, TN
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers
26 of 30 people found this instruction helpful.
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Dryer would not tumble.
I wasn't sure if the problem was the belt (probable) or the idler pulley assembly (less likely) but the total for both parts was about $26 plus shipping. So why not replace both to be sure?

As it turns out, my original idler pulley assembly does not turn. Rather, it has a concave semi-circular piece that is fixed in place. The belt ran in a groove in that piece.

The replacement part has a nylon wheel that turns. As a result of replacing the idler pulley assembly (which I don't think was necessary to fix my tumbling problem) the dryer runs much quieter. (We used to get a fair amount of squeaking when the belt rubbed).

As for the actual repair (I would rate myself as above average on tackling household repairs), it was about the simplest repair I've ever done. I followed the video provided on this site (excellent video) and it took less than 20 minutes -- cleaning up all of the lint/odds and ends under the washer and dryer took longer than the actual repair.

My only issue (minor) was disconnecting the electric harness. It did not slide as easily as in the video. I had to coax mine a bit with a small screwdriver (make sure your dryer is unplugged!!). I suspect it was simply a function of the harness never being unplugged -- the dryer is 9 years old.

I also felt great because I'm sure I saved a $125 service call (for only $26 in parts and 20 minutes of my life).

Good luck!
Parts Used:
Dryer Idler Pulley Assembly Dryer Drive Belt
  • John from Minneapolis, MN
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Screw drivers
24 of 25 people found this instruction helpful.
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Convert gas dryer to Propane
Received conversion kit. Removed front dryer panel,2 screws. Removed burner tube, 2 screws then removed natural gas orfice.
Installed propane orfice and repalced burner tube.
Removed regulater plug and replaced with new plug from kit using 90 degree ratchet screw driver. Approximately 20 minutes. Dryer working great.
Parts Used:
Dryer Liquid Propane Conversion Kit
  • Leonard from Lemitar, NM
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Socket set
25 of 30 people found this instruction helpful.
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Scratches in Surface
This product comes in a bottle with a brush like Liquid Paper. It goes on incredibly easy. A second coat might be needed. I wanted to prevent rust from setting in so I covered the scratches and dings. The paint is a little brighter since my washer is 10 years old but it still looks great.
Parts Used:
Refrigerator Touchup Paint (White)
  • Michelle from Richardson, TX
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
75 of 181 people found this instruction helpful.
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Dryer would quit before the end of the cycle
My wife reported that the dryer was not working. I checked it and it seemed to work fine. This went on for about a month or two. Every time I checked it, it started just fine.

Well, she threatened to go buy a new dryer, I took her more seriously. I thought perhaps a thermal protection was the cause. But when I dug into it, I learned that when those trip out, they are permanent (have to be replaced).

I finally noticed loud humming sound the motor made at start-up, when it failed to start turning on one occasion and eventually tripped out the motors thermal protection.

I ordered the new drive motor form PartSelect.com.

Replacing the motor was fairly easy if you like to take stuff apart. One thing that I had not anticipated was that the two foam gaskets on the exhaust duct were dry rotted. I went to my local part supplier to get them. They did not have them in stock. :( While I was there, I asked how much the motor was, they wanted $50 more than PartSelect.com :D

I put it back together without the new gaskets, and it runs like new. I ordered the gaskets from PartSelect and will add them when they arrive.

My wife is happy again, she can bust out the laundry in one day; it had been taking here all weekend.

I learned to take her at her word.
Parts Used:
Dryer Drive Motor w/Pulley
  • Ernest from Beaumont, TX
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Wrench (Adjustable)
24 of 28 people found this instruction helpful.
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Dyer would not heat, flame would shut off within 10 seconds
I opened the panel, undid the plugs, detached the radiant sensor by undoing one screw and removed and replaced the part. Fairly simply.
Parts Used:
Dryer Radiant Flame Sensor
  • Christy from Riley, MI
  • Difficulty Level:
    Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers, Socket set
24 of 29 people found this instruction helpful.
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The old lint screen on the dryer was broken
I analyzed the situation to see how to remove the old lint screen. I carefully pulled out the old lint screen. I was careful not to drop it. With caution, I placed the old lint screen in the trash receptacle that was nearby. Next, I opened the box that the new lint screen came in with a sharp knife. I removed the new lint screen from the box, took off the plastic wrap and inserted the lint screen in the same slot that the old one used to be in. I tested that it was seated correctly by pulling it out and reseating it in the slot. The true test came when I ran my first load of laundry through the dryer. The total repair time for this fix was 14.92 seconds.
Parts Used:
Lint Filter
  • Bill from Farmington Hills, MI
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
24 of 29 people found this instruction helpful.
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dryer stoped heating
the problem was not the igniter its was the thermal fuse I broke the igniter during inspection of the problem be careful its a very easy thing to break repairs complete thank you parts select for the quick shipping and low prices
Parts Used:
Dryer Igniter Kit
  • valerie from Elasmore, KS
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver
23 of 26 people found this instruction helpful.
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The dryer belt broke. During the effort to replace the belt it was noted that the lint trap housing seals were in need of replacement.
With the dryer taken apart to replace the broken belt it was obvious that the lint seals had not been working properly due to the excessive amount of lint covering all of the inside surfaces of the dryer. The belt idler pully had also moved from its normal mounting position and was laying at the bottom of the dryer. Because the lint had covered the bottom before the belt broke it was obvious to determine where the idler pully attached to the bottom.

Before cleaning I marked the exact location where the idler pully mounted to the bottom of the dryer.

While waiting for the replacement parts to be delivered a vacuum cleaner was used to remove lint from the inside surfaces of the dryer as well as the old fragments of the lint trap housing seals were removed and surfaces where the new seals would attach were cleaned.

Assembling the dryer with the new belt was a challenge due to the lack of support for the drum while getting the new belt in place, lined up properly, threaded through the idler pully and attached to the motor drive shaft. This is how I installed the new belt:

I used a piece of wood wider than the sides of the dryer, drilled holes that allowed for a piece of cloths line rope to be looped through and used to support the door opening end of the drum.

The drum was set on the seal and rollers at the back of the dryer.

The temporary wood /rope hanger was placed at the front end of the dryer resting on the sides with the top of the dryer raised.

The rope was adjusted until the drum rested on the back rollers and the rope like it would be positioned normally.

The new belt was then gently installed under the temporary support rope and around the drum.

The new belt had many kinks from shipping and was difficult to align with the location on the drum where it needs to ride so small strips of tape were temporarily used to hold the new belt in position until it could be fed through the idler pully and on to the drive shaft.

Several small pieces of a cardboard box were used to shim under the idler pully to hold it in its proper location as well as to make the belt attachment to the drive shaft easier.

With the belt attached, the temporary cardboard shims were removed from under the idler pully.

The front of the dryer was attached .

The temporary board and rope hanger was removed.

The tape that had been placed over the new belt to hold it in proper alignment was removed as the drum was rotated slowly by hand to ensure that all tape was removed prior to closing the top of the dryer.

The seals as well as the remainder of the dryer assembly was completed without any problems.

The dryer ran well for its initial trial spin and has dried several loads of laundry since.

Great parts and support Thankyou
Parts Used:
Dryer Seal Dryer Lint Trap Housing Seal Dryer Drive Belt
  • Benjamin from WELLS, ME
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver
23 of 26 people found this instruction helpful.
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Belt broke, dryer stopped.
Replaced the belt and the wheels supplied with the kit. I also cleaned the inside of the unit. It looks and works like new.
Parts Used:
Dryer Maintenance Kit
  • Richard from Groveland, MA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Nutdriver, Screw drivers
24 of 30 people found this instruction helpful.
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Push start and the motor would hum.
**** Remove power cord from the wall****

As said earlier, you will need to lift the top. Drop the two screws holding the lint shoot and pop the top by sliding a screw driver into the corner on the front. Lif tthe top and rest against the wall behid the unit. remove the two (4 total) screws at the top and bottom of the front door assembly.
Place sometin under the front portion of the drum. At this point you'll see the need to clean everything! :) Slide the belt off and around the drum, (take note of the routing it takes.) Remove the drum by gently pulling it towards you. Set it aside. Clean more. :) (It is nice to have a vacuum handy.) At this point you really need to get to the rear of the system. So I tipped the top back down, and spun it around. Removed the rear panel and cleaned some more. (15 years of a lot of lint in there!) Then you'll need to remove the rear cover on the left side, covering the blower impeller. Get read for a whole lot of debris. Vacuum again. So now you have the motor exposed in the front and rear. You need to remove the impeller by turning that clockwise to loosen it. The trick is holding the shaft in place from the front at the same time. I used an old rag and wedged it into the impeller edges and worked it around until it jamed up. Once the rag was wedged pretty good, I went back to the front spun the shaft. Then you can remove the impeller by hand. Vacuum more. You may get by without having to remove the lint shoot completely, but I did just to clean it up more. I did have to remove two screws in the upper corner near the top of the lint shoot. (Basically the hold the back in place.) I took a few notes at this point about the wiring harness. Used a heavier screw driver (standard), You can push down on the clips that hold the old motor in place. Then work it out the front. Clean more. The new motor is not an exact replacement slightly differnt but the instructions with it were ok. Follow them for the correct wiring. You will need to remove one wire and cut and recrimp a spade lug or two. I used ty-wraps to secure the lines back in place. Look closely at the diagrams and make sure you set the motor down in the same direction the instructions say, if you twist it slightly it will sorta lock in place where it needs to be. Re-install the hold down clips to the front and rear of the motor. Clean up your impeller, and reinstall it too. Then basically reassemble the dryer...tracing your steps backwards. This isn't really difficult, it just takes time and as you can see, you will/should clean as you go !
Parts Used:
Dryer Drive Motor w/Pulley
  • Doug from Manitowoc, WI
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Screw drivers, Socket set, Wrench (Adjustable)
22 of 26 people found this instruction helpful.
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timer wouldn't advance dryer wouldn't shut off
Took the back off the dryer control panel, unscrewed the old timer, unplugged the wire leads from the old timer and put them on the new timer. Then I screwed the new timer in place of the old one and replaced the back panel cover. one nut driver did the whole repair. about ten minutes tops.
Parts Used:
Timer - 60Hz
  • Larry from Okemos, MI
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Nutdriver
21 of 24 people found this instruction helpful.
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The dryer was making a squeaking sound when running
Installation went very well. Raised the top of the dryer, removed the front of the dryer, remove the drum, at this point the dryer‘s wide open removed the police and the tensioner also remove your tire rings replace everything back in order as how are you get apart. Repair took about an hour and 15 minutes
Parts Used:
Dryer Tri Ring Dryer Maintenance Kit Dryer Rear Drum Support Roller Kit
  • David from PATASKALA, OH
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers
21 of 24 people found this instruction helpful.
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The dry was getting hot but not for long, then not at all.
Once the coils for the gas valve got hot they failed and shut the gas vavle off, we ended up changing the coils which fixed the problem but part select held up there end of shipping out these parts which we could not get localy. so if your dry ignites some time and or not for long its either these coils or the cycling thermostat which will casue the same conditions because the the cycling thermostat controls the coil. good luck!
Parts Used:
Thermal Cut-Off Fuse Kit Dryer Internal bias Thermostat
  • brendan from brick q, NJ
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers, Socket set
29 of 49 people found this instruction helpful.
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The Dryer Would Not Turn On
The dryer wouldn’t turn on at all. It was like it was unplugged from the wall. However, fixing it couldn't be easier. I simply removed the back panel, found the fuse, tested it with an Ohmmeter (to determine that this was the part that didn't work), ordered the part from this website, and replaced the part. The part arrived in about two days. The shipping was a little pricey, but overall the whole thing cost me $20 vs. whatever it would cost me to get someone else to repair it. The website helps to identify the problem, and it is helpful to read how other people fixed their problems. It was so easy and the service was so good, I will definitely use this website again and recommend it to others.
Parts Used:
Dryer Thermal Fuse
  • Ribhe from Wildwood, MO
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Nutdriver, Screw drivers
19 of 19 people found this instruction helpful.
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All Instructions for the 7MWGD1602AW0
46 - 60 of 1632